The Short-Circuit Amplifying Technique.
By Charles Douglas Wehner |
28 July 2003 |
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PRINCIPLES
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This story begins in the very early seventies. There was news in the
technical press that there was a strange oscillation to be found
AT SOME ULTRASONIC FREQUENCY
in a small-signal silicon-planar transistor whose collector was shorted
to its base. |
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The author was aware that at normal temperatures, such as 20°C or
68°F, and one milliamp of current, the base threshold will be about
0.6v with +58mv per decade. The collector will saturate at about 0.2v.
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It was precisely for this reason that the author was in the habit of
biasing his amplifier stages - even within multivibrators - by means
of feedback from the collector and not directly from the supply.
Rising gain at low temperatures can no longer stop the amplification.
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So even with the base-bias resistor reduced to NIL, there was headroom
enough at the collector for the device to amplify. Had the reporter
been sloppy in his work? Has a tangle of wires generated uncontrolled
parasitic inductance and capacitance?
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SUPER-REGENERATIVE V.H.F.
The explanation was correct. The author set to work, and within a day
had created a radio receiver where there were only three turns of 15 SWG
wire between the collector and base of the first transistor - and yet
that transistor did not just amplify, but
OVER-AMPLIFIED.
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VT1 was nothing special - various devices such as 2N2926 were tried,
with virtually identical performance. Most silicon devices,
even in the seventies, had an Ft of 200MHz. or more.
Yet, with R1 set to 8.2 megohms, and a supply as low as 1.2v,
this SUPER-REGENERATIVE design
would squeg. Overamplification meant that the R.F. would rectify
at the base of the transistor, until the drop in voltage on C1C2 caused
the oscillation to stop.
There was then a pause whilst the voltage recovered via R1.
Broadcast signals coming down the antenna would modulate the squegging
delay, which in turn would modulate the D.C. on R1. This was in
turn amplified by a single stage, VT2, which itself used only a
microamp of current.
With a high-impedance piezo earphone, the design gave good volume at
intelligible quality - despite the HISS that people
associate with FM. This hiss is actually a fault, but a FEATURE
in low-current super-regen designs like this.
Whilst setting it up, the author heard the audio of British BBC1
television at about 45 MHz., taxi-cabs from the other side of
London at about 75 MHz., the entire 88-108 MHz. band, and the aeronautical
weather station at about 160 MHz.. Pilots thirty miles away
approaching Heathrow airport were also heard
COMING UP ON THE LOCALISER NOW.
The design runs non-stop for about two years on a single tiny watch
battery.
A gadget had been made that deliberately
stretched incredulity to the limit. Minimum components, absurdly low
current, frequencies close to the cut-off limit of the transistors,
and yet the design was conspicuously bursting with activity.
SUPER-HETERODYNE A.M.
It was decided to try something more ambitious.
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When this A.M. radio design was tried with Weyrad coils from Weymouth
Radio, it proved to be a complete non-starter. However, a change to a
standard coil-set from TOKO, a Japanese
company, resulted in instant success.
Second-sourcing was possible at that time from
SAN ESU, a Hong Kong company who made a similar coil-set.
However, I understand that they were taken over by Toko.
L1 was home-made. It was a coil of a few hundred turns wound onto a
standard ferrite rod. The secondary, L1a, was about fifty times less.
This coil was made in such a way that it would cover the medium waveband
of 550 to 1500 kiloherz with a standard double-ganged variable capacitor
VC1. The fitted padders and trimmers are not shown.
Whilst transistor VT1 amplifies the aerial signal in common-emitter
mode, it also oscillates in common-base mode with the standard Toko
oscillator coil L2.
Intermodulation produces the Intermediate Frequency, which I believe
was 455 kiloherz, that is trapped by I.F. transformer L3 and fed via
L3a to I.F. amplifying transistor VT2.
Another I.F. transformer L4 feeds via L4a onto the second I.F. amplifier
VT3. NOTE THAT THE CURRENT TAKEN BY VT2 IS
ALSO USED BY VT3.
The standard output coil L5 feeds the detector VT4. Here, instead of
a collector-base short we have an emitter-base short. Yet there is
adequate signal to give a reliable detection.
C4 promptly suppresses the R.F. component out of the audio.
The biasing behaviour requires some study:
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Mixer supply
It will be seen that as the collector of VT1 is shorted to its base,
the device from a DC viewpoint can be considered to be a 0.6v Zener diode.
Similarly, the two I.F. amplifiers VT2 and VT3 act together as a 1.2v
Zener diode.
The first thing to be seen, therefore, is that at no added expense a
STABILISED POWER SUPPLY has been
set up for the self-oscillating mixer.
R1 was chosen to be 680 ohms, so that the self-oscillating mixer was
running at just under a milliamp. For ultra low noise, this current
can of course be increased. This is because at 0.6v and one milliamp
the devices dissipates just 600 microwatts of power, leaving plenty of
room for customising.
Audio bias
That milliamp or so passes also through R3. We can calculate the
voltage-drop across R3, and subtract it from the power-supply volts.
This is the highest that is possible with the given values
of R1 and R3. Let us call it Vmax.
If we now disconnect VT4 in our imagination, we will
find extra current flowing down through R2 and R3. This defines the
mid-point potential at the junction of R2 and R3. Let us call this
Vmid.
Let us now reconnect VT4 in our imagination, and think of a steady
I.F. signal obliging VT4 to take that extra current instead of it passing
through R2 - which only carries the mixer milliamp. This is the
situation when there is an EXTREMELY
strong signal.
A.M. signals are symmetrical. Thus, the troughs in the I.F. signal that
allow the collector volts of VT4 to rise to the upper limit are matched
by peaks that allow VT4 to fall to its lowest point.
Accordingly, if (Vmax-0.2v.) is less than
twice Vmid the detector VT4 cannot saturate
on symmetrical signals.
That it saturates briefly on sudden non-broadcast bursts, such as due
to an unsuppressed motor-vehicle, is actually a bonus. There is headroom
at the detector for the official broadcast, but noise is clipped.
A.G.C.
R2 and C3 form an integrator, which removes the R.F. signal from the
I.F. amplifier supply line but also removes the high-frequency component
of the audio. The 3dB point will generally be chosen to be at about
100 to 150 Herz.
This smoothed signal now passes through BOTH I.F. amplifiers.
This gives powerful A.G.C. over the entire R.F. strip
The behaviour under conditions of variable signals is worthy of note:
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If the I.F. strip is taking a milliamp, both transistors act as
resistors of 600 ohms. However, on a stronger signal that pulls
down the A.G.C. and delivers only a tenth of that, the transistors
behave as if they were about 6 kilohms.
Accordingly, VT3, C2 and VT2 behave like a
T-network with a time-constant that is long on
strong signals that deliver low I.F. current, and short on weak ones
that allow the I.F. current to rise.
The Kennelly-Heaviside layer is known to fluctuate. In the early
days of Radio Luxemburg, when radio engineering was not so advanced,
listeners in London were often frustrated by the rapid flutter of
the sound under some conditions.
The variable A.G.C. time-constant of this design allows the bass
to be received on strong local signals whilst sacrificing some of
it to receive weak, distant, unstable signals at good quality.
These points were planned into the design, and confirmed by the
prototype.
A 75 ohm loudspeaker was substituted for R3, and the design delivered
a reasonable volume of sound - but with no control of volume other
than by detuning.
CLOCKWORK
It was at this point that the author decided, in 1976, to attempt to
run this radio from CLOCKWORK.
This would normally be considered to be nonsense, but the extreme
power economy of this design meant that it could be tried.
A typical 12-ligne mens
wristwatch - even when analogue, and therefore full of wheels -
can run on a mercury battery for up to three years. The mainspring
and drum of a mechanical watch are about the same size, but can
manage only a single day.
It was realised, therefore, that the energy-storage capability
would be about a thousand times less than with a chemical battery.
A broken clock was taken, and the balance-wheel removed. Its minute
hand was connected by means of heat-shrinkable sleeving to the shaft
of a TKK Mabuchi model motor. The terminals of that motor served as
the power-supply to the above radio.
When the clock was wound and allowed to run, the motor delivered
sufficient power for several seconds of sound from the radio.
The radio was tried with a high resistor at C3 and a piezo earpiece,
and with a 75 ohm loudspeaker in that position. Both worked.
The motor appeared to deliver volts that were a reasonable
approximation to a linear decline, so that the volume declined
according to an approximate square law. This severely compromised
the usefulness of the device.
Studies were made of the rate of run-down of the clockwork mechanism.
It was clear that on light loads the mechanical system would run for
about twice the time. The back-EMF from the motor was slowing the
clockwork. However, the clockwork could
NOT - of course - be brought to rest or there would be no back-EMF.
It was decided that a mechanical BRAKE
must be fitted to the clockwork, so that when the volume-control is
set to nil the clockwork stops and its stored energy preserved.
It was also observed that attempts to wind the spring whilst the
system was running would cause the drive to be removed from the
motor, so that the volts would stop and the radio would become silent.
It was immediately realised that the whole idea of a clockwork radio
was therefore impracticable. A system with a rechargeable chemical
battery, charged directly from the generator, would be better.
It was further decided that a small transformer and rectifier could
provide the additional facility of recharging a battery from the
domestic supply. There was no such easy way of rewinding a spring.
Again, a chemical battery could be easily recharged from a solar
cell, but there was no such way of rewinding a spring from sunlight.
In a patent application by the author for the short-circuit amplifying
technique, mention was made that the power economy was so low that the
radio had been shown to work EVEN FROM
CLOCKWORK, but no claim was made for the invention of the
clockwork radio because its technical shortcomings made it a
worthless idea.
In the English Daily Mail newspaper, a man who gave his
name as Dr. claimed that he had been granted a patent
for the clockwork radio in 1985. He quoted the patent number.
In the later 1990s, a man who had formerly been begging on the streets
of Berlin demonstrated on Tomorrows World on BBC
television, a radio that ran for a few seconds from clockwork.
This design consisted of a piece of formerly-discarded
clockwork, a motor from a broken toy and the circuit panel from a
broken radio.
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There exists a DISGUSTING
GANG in London, who specialise in creating disgusting
people like Saddam Hussein.
They look for some small thing that you are ashamed of. Then, with
threats of publishing and of punishing you, they force you to become
filthier and filthier.
These are the DARK FORCES
that the Queen spoke of.
Members of the gang had already put pressure on Nelson Mandela to send
his civil service to London for training.
Had he agreed, his civil servants would have returned to South Africa
full of guilt and the fear of exposure. They would have been British
puppets.
On seeing the beggar on television, the gang rushed to him. Do you
believe in the Immortal Spirit? Do you believe in the Everlasting Soul?
You could be an important man!
The beggar discovered a sudden enthusiasm for religion. He instantly
acquired the Presidential Gold and Silver medals of the Institute of
Electrical and Mechanical Engineers. He instantly received the title
of Master of Science from Brunel university, and became a visiting
PROFESSOR at Buckingham university.
He was wined, dined and filmed at Buckingham Palace.
Bristol university was given millions of pounds of tax-payers
money to make a viable clockwork radio from the prototype.
A charity in South Africa was pressured into liberating large sums for
the setting-up of a clockwork-radio factory.
We use CRIPPLES because they
are cheap will have been the mentality. The disgusting gang told
the world that they provide jobs for the
DISABLED.
The beggar cried tears of joy when he saw that factory. On television,
he explained that it had been such a tremendous battle before his
GENIUS had finally been recognised.
He was unaware that he was being USED.
At the big presentation of a clockwork radio, the beggar was introduced
as Professor Clever. He smiled the way he had been trained
to smile, and coaxed Nelson Mandela into turning the mighty wheel.
Bristol university had put in a TITANIC
spring as a solution to the energy-storage problem. The ratchet-wheel was
of TITANIC proportions, as was the
pawl.
The wheel refused to budge.
Professor Clever urged Mandela to have another try. The Elder Statesman
of Africa pushed with all his might, and suddenly.....
CLUNK!
This was the moment that nearly changed world history. Had the clockwork
radio done for Mandela what years of imprisonment had failed to achieve?
Mandela sat there in a state of SHOCK.
His heart was obviously fluttering - but would it stop?
No. He recovered, and the world was saved.
Thats VERY NICE
, he mumbled without conviction.
The clockwork radio factory promptly went bankrupt.
Professor Clever was ALLEGEDLY paid
off with £180,000 (Sterling).
However, on joining the gang you swear an oath not to do anything
without permission. He lives in hope of being allowed one day to spend it.
He went on to invent the CLOCKWORK
COMPUTER, in which you wind the
TITANIC spring for 24 hours and get
an uninterrupted 20 seconds of computing bliss before the system
crashes, and you lose all your data.
In the (London) Daily Mail he lamented I telephone my
colleagues in South Africa, but they REFUSE TO RETURN MY
CALLS....
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Voltage tuning
One variant that was planned - but not fully explored - was the
use of a digital system to control the tuning. This would use voltage
tuning.
It is known that the thickness of the depletion region in a silicon
diode varies directly as the reverse voltage - but only when that
reverse voltage is measured from the 0.6v threshold point.
Devices have been made with special mesas, and neutron doping,
in order to defeat the natural law of the diode. Such specialised
diodes have a linear law for use in such circuits as the Wien bridge.
However, Nature seems to be telling us something about good design.
At low voltages, the frequency of an LC tank circuit (where C is a
varicap) varies reasonably linearly with voltage.
Consider the following circuit alteration:
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Here, with nil tuning volts, DV1 is forward biased to its threshold.
It is just conducting, and the L1DV1 frequency is nil.
DV2, on the other hand, has NIL bias. Its capacitance is what one would
expect to measure on a capacitance meter with a disconnected device.
This, together with L2b, should be set to the I.F. frequency (455 kHz.).
So now we raise the tuning volts to 0.6. L1 was designed so that L1DV1 now
delivers 455 kHz, and as the width of the depletion layer of DV2 is doubled,
its capacitance has fallen by a square law to a quarter and the
L2bDV2 frequency is 910 kHz.
So it goes on, with a fixed 455 kHz difference. The system allows
voltages from 0.659 to 1.978 to cover the medium-wave band of 500
to 1500 kHz.
Higher frequencies are possible at higher volts - but the inverse
square law of the diode acquires some inverse cube law. In addition,
the parasitic capacitances become more significant as the varicap
capacitance decreases.
The concept is just one of a series of ideas conceived for the
simplification of production - with no padders and trimmers to
adjust.
Whether the volts come from a potentiometer or a digital system depend
upon the manufacturers design specification. A digital circuit can,
for example, be frequency-stabilised by a huff-and-puff system.
SUPER-HETERODYNE F.M.
The viability of amplification in the region of 100 MHz. had been
proven with the very first design. However, it was time to try to
compete with the best of the F.M. superhets.
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L1 and L2 were home-made coils of a few turns of stout wire. The first
stage, VT1, is again a self-oscillating mixer. Separate oscillator and
mixer circuits could have been built, but this was not tried.
L3 and L4 are standard TOKO 10.6 MHz I.F. transformer stages. The
author had many of these, and decided to use them in positions L5
and L6 as well.
A Travis or Foster-Seeley discriminator could have been constructed,
but WHY USE PASSIVE DEVICES?
Instead, L5 and L6 are detuned to the lower and upper sidebands of
the I.F. signal. The detectors VT4 and VT5 then give detection with
gain.
VT4 and VT5 form a LONG-TAILED PAIR
with R3, which helps linearise the output - but there is MORE.
The A.G.C. is ULTRASONIC.
What this means is that the time-constant R2C3 is made less than a
sixty-thousandth of a second. The 3dB roll-off point will be at about
10 kiloHerz.
So any mismatch between devices VT4 and VT5, as well as any A.M.
breakthrough, will be cancelled by the A.G.C. at audible frequencies.
C2 is also made small, so that it creates a similarly short time-constant
with transistors VT2 and VT3 at their nominal current of a milliamp
(600 Ohms). The overall effect is an astonishing level of A.M. rejection.
It did not escape the authors attention that having switchable
capacitors in positions C2 and C3 would allow the same I.F. strip to be
used for A.M. and F.M. in a dual-standard design.
At the detectors VT4 and VT5, resistors R4 and R5 are chosen to make
saturation impossible. This was described for the A.M. design above.
Capacitor C4 forms with R4 - and C5 with R5 -
a time-constant to match the de-emphasis standards of the broadcasting
authorities. This will be 50 microseconds
in Britain, and 75 in the U.S. and
Germany, for example.
The symmetry of the detectors was maintained not only to maximise the
A.M. rejection, but also for studies of push-pull output applications.
R6 and R7 are megOhms, compared with the kilOhms of R4 and R5. They form
with C6 and C7 a time-constant of about a tenth of a second. Thus, if the
lower sideband is too strong the volts on C6 will feed to the anode of
varicap diode DV1 in such a way as to raise the frequency of the oscillator.
Similarly, if the upper sideband is too strong, the capacitance of DV1 will
increase.
C8 is just a picoFarad or so - it consists of a couple of pieces of
lacquered wire, about a quarter of an inch long, twisted together.
A positive A.F.C. lock was detected.
In addition, a study was made of the extraction of stereo sound from
the system:
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Here we see how the unused side of the discriminator delivers the
pilot-tone to a coil, L7, tuned to 19 kiloHerz. Transistor VT7 is turned
on whenever that tone appears, and the red LED lights up.
But the half-wave rectification of the 19 kiloHerz tone generates a
high level of second-harmonic signal at 38 kiloHerz, which is trapped
by L8.
The secondary of L8 is strapped between the bases of TWO transistors,
VT5 and VT6 where in the mono design there was VT5 alone.
In this way, the bases of these two transistors have a composite of
I.F. and 38 kiloherz upon them. One will be biased off to leave the
other to detect the signal, and then the action rocks back to the other.
The author was working on this design when he was disturbed by somebody
knocking at the door.
COME IN, he called. Nobody responded.
Again there was a knock. Again, the author called out Come in.
Then a great drama unfolded - and it was indeed a drama. It was the
sound-track of British television.
This kind of experience shows that the electromagnetic environment in
the V.H.F. region is extremely quiet. Yet, years earlier, when working for
the British Radio Corporation, the author had always experienced V.H.F.
designs to hiss.
What was becoming clear was that the cause of the hiss was not in the
environment - but POOR NEUTRALISATION OF THE
I.F. STAGES.
The short-circuit design, with dozens of biasing resistors and their
bypass capacitors removed, has such simple lay-out that neutralisation
is rarely a problem.
However, a shortage of ready-made coils and of time to create hand-made
ones meant that the stereo converter was never perfected.
When the stereo was switched on at the transmitter, the red led lit as
expected. The hiss level increased from inaudible to noticeable. The
stereo discrimination, however, was uncertain.
Had a viable stereo-pair been achieved it could have been improved.
This could be arranged as follows:
If there is ten percent of left in the right, and ten percent of right
in the left, you add ten percent of the
ANTIPHASE signal from whence you took the pilot-tone. This leaves
the left and right pure, and at 90% of their original voltage.
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The author had come to Britain in 1973 to stop the country from
starting trade with the Common Market.
The reason was that the parity of Sterling was three times too low.
By 1976 it was already SIXFOLD undervalued.
A major economic calamity was about to unfold.
The author had been unaware that there was a
disgusting gang who were forcing through this trading
agreement simply to ROB EUROPE.
The author was unaware that the eminences who
delivered learned economic advice were just beggars
and thieves like Professor Clever.
So the author broke off much of his electronics research to attend
to trying to save British industry - and to avert a world recession.
The Professor Clevers failed to understand the warnings.
The Queen signed for trade in 1977. All industry collapsed. The author
fled to Europe, because he anticipated some kind of Winter of
Discontent. That winter came in 1979.
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U.H.F. MODULATOR AND PATTERN GENERATOR
Just before leaving the country, the author decided on one last
experiment - to take the technique up close to a gigaHerz.
A television test-pattern generator was made, in which the R.F.
modulator had a half turn of printed coil. Lecher lines were not
attempted, because these have a sharp resonance. After all,
the purpose was to cover the 430 to 860 megaHerz band.
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The British line-standard is 312.5 lines at 50 fields per second.
The American is 262.5 at 60. Thus, the British line-rate is
15625 per second where the American is 15750.
L1 was a standard 455 kiloHerz I.F. transformer with a capacitor
added to pull it down to 156250 Herz. It forms a short-circuit
oscillator with VT1.
The decade-counter IC1 delivers ten patterns of binary at its
four outputs. It is a 7490, which has a divide-by-two stage
and a divide-by-five stage. The linkage that converts this to
a divide-by-ten is not shown.
Normally, the four outputs - units, twos, fours and eights -
would be connected to resistors of say, eight, four, two and one
kilOhms. Then, a regular staircase is generated.
However, such accuracy was not needed. "Preferred values" from
the European E12 series were chosen instead, and the eights
bit was deliberately given an excessively low resistor.
The result was as follows:
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British television uses negative vision modulation, where black is
presented as a high voltage. Sync pulses are higher still -
BLACKER THAN BLACK.
This waveform delivers eight bands across the screen, with the
brightest on the left. The vertical timebase was allowed to
run free.
In a basement full of colour televisions, all tuned to a standard
broadcast, the appliance was switched on. About fifteen television
receivers simultaneously switched over to show the grey-scale.
Experiments were done throughout the 430 to 860 megaHerz band.
The performance was consistent throughout.
A Phillips colour test-pattern generator was plugged into the
socket. All televisions then showed the colour pattern. Here,
the vertical timebase was properly synchronised.
Since that time, many people have manufactured modulators to
cater for the computer craze. The earliest home computers were
designed to display their output on the domestic television.
However, throughout that period nobody marketed a product with
a modulator as simple as this - printed coil L2, transistor VT2,
tuning capcitor VC1 (a single blade on the circuit-board,
insulated with mica) and bypass capacitor C2.
Indeed, although the designs shown are considerably cheaper and
better than the established circuits, at no time in the thirty
years since they were conceived was anything resembling them put
on the market.
A silicon transistor might give a minimum current gain of 50 - or 17dB.
Depending on the design, in common-emitter mode it might also deliver
a similar voltage gain. Thus, 34dB should be available.
Resistive coupling between stages causes much of that gain to be
wasted - whilst resistor shot-noise is added.
Transformers are one of the most efficient devices conceived by Man.
They contribute negligible noise, and can convert the voltage gain
into current gain. Thus, with optimum matching of the transformer
to the transistor one transistor delivers the performance that
would require two in a resistively-coupled circuit.
All of this spells low noise.
Even though the advances in integrated-circuit production have led
to radios being cheap and easy to manufacture, there is room at the
top end of the market - the Hi-Fi and low-noise sector - for designs
using coils.
The extensive use of robotics in production also makes the concept
commercially viable.
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A typical mass-produced gain-block might contain the standard coils
together with a mechanical resonator - as marketed by Toko. But it
would be extended by incorporating a low-noise transistor matched
to the turns-ratio of the transformer.
The secondary of the transformer might be unconnected - as shown -
to allow the designer to connect it to either power rail, the ground
or Vcc.
During the period since the designs were conceived, many advances
such as the development of Standing Acoustic Wave (SAW) devices
took place. They make a useful alternative to the mechanical resonator
or crystal.
MORE ADVANCED USES
As these amplifiers require minimum volts - just over 0.6 when
powered directly from the supply or just over 1.2 when cascaded -
they can be run from high currents. This reduces the quantum noise
of the electricity.
The signal is presented via a transformer to a transistor, transformed
into the next transistor, transformed into the next and then
transformed into the detector. There is nothing else in the signal path.
The bypass capacitors on the power lines suppress the resistor noise.
Accordingly, one begins to think of uses for the concept in special
amplifiers for radioastronomy. They might offer a commercially viable
alternative to maser and photomultiplier systems.
Yet, at cryogenic temperatures (solid carbon-dioxide or even liquid
helium), there is the possibility of gas-bubble formation. When designing
amplifiers for very low temperatures, this should be borne in mind.
In addition, the transistor gain rises as the temperature falls - a
bonus, when designed for. However, the threshold of the transistor
rises from 0.6 towards about 2 volts. The author does not any longer
have access to his reference material to quote exact figures.
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In a microprocessor-controlled application such as Rahman Spectroscopy,
a gate such as the field-effect transistor FET1 may be incorporated.
A pilot burst is sent through the amplifier to stabilise its gain.
Then the gate is closed whilst the feeble signal is detected.
In this way, the gain can be made independent of the signal.
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The author returned to Britain in 1983, to find all industry gone.
He bought a house in Wales, and the British government immediately
set about encouraging crime. Perhaps a ton of industrial components
- transistors, resistors, capacitors, circuit boards, connectors and
other parts - were destroyed. The authors antiques were also
variously stolen or destroyed.
It made no difference to the disgusting government that the author
had delivered the key information that saved the economy in 1985.
Industrial prototypes were wrecked. Optical devices and large numbers
of patent scripts were demolished.
The author, having lost his home, sought refuge with a good landlord
in Hampstead, London.
Then the disgusting gang bought out that landlord cheaply,
and illegally evicted everybody.
THEN CAME THE 11th OF SEPTEMBER.
The disgusting government were now thrilled. They had the excuse they
needed for WAR. Orders seem to have gone out to KILL SOMEBODY.
People who have already killed in England make better killers when
they are sent to Iraq.
The government had created vast numbers of fake doctors. Harold
Frederick Shipman was a drug dealer who was dressed-up as a doctor.
He was taught to kill in a hospital, where the other fake doctors
killed the patients with heroin.
The authors own father, Dr. Carl Heinrich Wehner, was killed
by disgusting doctors using heroin in a hospital in Dulwich, London.
Therefore, when the newspapers reported that there were 50,000
INVOLUNTARY EUTHANASIAS every
year in Britain, the author realised that this is true.
The principle of the disgusting gang is to commit crime on such a
huge scale that nobody will believe it.
Shipman had a huge salary going into his account, but was not allowed
to spend any. Living in poverty, Shipman developed a
PIGGY BANK obsession. He killed
862 people - mainly old ladies - just for the contents of their
piggy banks.
The rapists Ledward, Alison and Walton were similarly installed as
fake doctors. They were described as Gynaecologist,
Psychiatrist and General Practitioner.
It seems that when the order went out to KILL, some members of the
gang who had only raped refused to be corrupted any further.
There was a spate of fake doctors being prosecuted during the
closing months of 2002, the above three amongst them.
A REAL doctor was sent to visit
the author, and she immediately diagnosed Addisons disease,
a very rare disease that she had nevertheless seen before.
There was, of course, a scam involved. Now the disgusting government
had a document that could be interpreted two ways:
1. The patient was ill, so there is no culprit.
2. The accused can be shown to have been in possession of the
document, and has therefore deliberately killed a vulnerable
person.
So the way was now open to arrange the murder and compromise the
murderer.
On 17th december 2002, the author was evicted onto the street.
Government documents were prepared that declared that he had
Made himself deliberately homeless.
The author had the fatal Addisons disease, plus sepsis and a
high temperature. The weather was well below zero, and it was snowing.
After a very close encounter with death, the author escaped into
Europe.
Against this backdrop, there is absolutely no hope for the author
to build any industry.
However, there are those on this planet who are well placed to put
the knowledge of the short-circuit technique to good use.
A man who has been robbed of everything by corrupt government is in no
position to hand out free gifts. However, such knowledge as is presented
here is only of use when it is USED.
The knowledge is given in trust to the world, that it be preserved
and used. As great savings can be made in industry, by rights a
percentage of profits should be held in trust for the author.
THE DESIGNS, WITH FEW EXCEPTIONS,
ARE FULLY TESTED AND PROVEN.
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It is not only bipolar transistors that can be short-circuit biased. There are
two kinds of unipolar field-effect transistor - ENHANCEMENT mode and
DEPLETION mode.
Enhancement mode transistors - as in COSMOS logic, for example - need to
be biased on. A DC short-circuit from gate to drain will do this.
The emphasis was put on the bipolar devices because their threshold voltage is
dependent upon the band-gap potential of silicon. This is defined by natural laws.
The threshold of a FET is more dependent upon device geometry, and not so easily
specified in a general article such as this.
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(C) 1973-2003 Charles Douglas Wehner.
Use freely but do not plagiarise.
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